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Homing does not work yet because I’m waiting for the micro switches to come in, as soon as I hit home it moves a bit and stop because there’s nothing plugged in and the firmware is reading high across all limitswitch pins.

But putting G1 Z10 does move it 10mm up. Approximately anyways, still need fine tuning etc.

So it’s odd that it would do these commands, and then release the motor right after move is complete. Could this be the little pot thing on the Printrboard? That’s the voltage reference for getting the right amount of current to the motors, does it affect the holding at all?